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I've got a 07 600HO motor in my IQR, and I rode it 1 time this past winter (sad I know, but I spent my other time on my 03 Blade Highlander). When I was out on my IQR, me and my buddy (on a m6) were riding pretty hard just beating trails. My sled was running pretty good, after about a 30 second shot of riding WOT it bogged, instantly I thought I blew it up. I had previously just cleaned my exhaust valves and torn the PTO side gasket, I used forma-gasket to fix my problem considering it was a Sunday and I was taking my sled out to college that same day. I thought that would work until I was able to get a actual gasket for it. Well, a we went out riding and it bogged real bad after being WOT, but still ran decent after that, a couple miles down the trail it died. I pulled the plugs and they didn't look like they'd gotten hot, they were still cardboard brown, I got it running again and rode for another 40 miles but it didn't seem like it was running right. I've already put the sled away for the summer just because of college and I'll be 2 hours away from it for my summer internship, I'm just wondering what anybody thinks about me frying my pistons because thats what I think happened. Help is appreciated. Thanks
Chad
Chad